Thomas Labus
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Recent activity by Thomas Labus
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Well, good news and bad news... I exchanged the drone and ran the mission going around the block. It ran as designed! The bad news is, now it will not even complete the POI mission. It seems like ...
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I ran it again today as well... it is definitely the drone being rotated rather than the gimbal being pitched. Is this something likely with Dronelink, or do you think I might have something wrong...
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I ran the mission again just now. For most of the path, it was more accurate than it has been. I did make a modification to the mission, I added that the Drone Heading also be path... However, whe...
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OK, I am still getting bad results even on the one going around the block. I have the gimbal pitch at -45, and the gimbal heading at 0 degrees heading. I have also slowed the drone down to 10mph in...
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Another test I can do is t set the gimbal to the heading instead of using POI and set marker in various locations to only change the pitch.
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I will try to make another video this afternoon. I will run the same mission in daylight, and then also do a manual flight with photos of the expected angle.
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I calibrated everything before the each mission, and my results are consistent each time I run it. The stunning part to me is that it is pointing left instead of right, not being just a touch off. ...
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Here is the link for that one... https://app.dronelink.com/thomas-labus/test/plan/PWHe1ubxo5qPwvTiJphg/vYjAaJp4AvBF6xiyumAe
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I double checked my settings on the one following the road, and I may have had the gimbal heading wrong there, it may have been set to north instead of path or heading.... however, the part after ...
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I meant to say a distance of 380' and 300' high.
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